欢迎访问《现代矿业》杂志官方网站,今天是 分享到:
×

扫码分享

现代矿业 ›› 2024, Vol. 40 ›› Issue (04): 136-.

• • 上一篇    下一篇

内蒙古某铁矿石选矿试验研究

为了高效开发利用内蒙古某铁矿石资源,在矿石工艺矿物学性质研究的基础上开展了
高压辊磨—湿式磁选抛尾—塔磨—磁选全流程试验研究。结果表明:原矿经高压辊磨制得-1 mm粒
级粉矿,在400 mT磁场条件下湿式磁选抛尾,获得了全铁品位36.63%、磁性铁品位为31.31%的湿式
预选精矿,湿式预选精矿经塔磨磨至-0.030 mm占95%,经1粗1精磁选获得了铁品位为65.78%、回收
率为66.22%的铁精矿,试验结果可以为该铁矿石选别流程确定提供依据。
  

  1. 1. 中钢天源安徽智能装备股份有限公司;
    2. 中钢天源股份有限公司

  • 出版日期:2024-04-15 发布日期:2024-08-13

Experimental Study on Mineral Processing of an Iron Ore in Inner Mongolia

In order to efficiently develop and utilize an iron ore resource in Inner Mongolia,on the ba⁃
sis of the study of the mineralogical properties of ore technology,the whole process of high-pressure roller
grinding,wet magnetic separation,tail throwing,tower mill and magnetic separation was carried out. The
results show that the - 1 mm particle size fine ore was obtained by the high-pressure roller grinding ma⁃
chine,and the wet pre-separation concentrate with a total iron grade of 36.63% and a magnetic iron grade of
31.31% was obtained under the condition of 400 mT,and the wet pre-separation concentrate tower was
ground to -0.030 mm accounting for 95%,and the iron concentrate with an iron grade of 65.78% and a re⁃
covery rate of 66.22% was obtained by one roughing and one cleaning magnetic separation,and the test re⁃
sults could provide a feasible process for the iron ore separation.
  

  1. 1. Sinosteel Tianyuan Anhui Intelligent Equipment Co.,Ltd.; 2. Sinosteel New Materials Co.,Ltd.
  • Online:2024-04-15 Published:2024-08-13

摘要:

为了高效开发利用内蒙古某铁矿石资源,在矿石工艺矿物学性质研究的基础上开展了
高压辊磨—湿式磁选抛尾—塔磨—磁选全流程试验研究。结果表明:原矿经高压辊磨制得-1 mm粒
级粉矿,在400 mT磁场条件下湿式磁选抛尾,获得了全铁品位36.63%、磁性铁品位为31.31%的湿式
预选精矿,湿式预选精矿经塔磨磨至-0.030 mm占95%,经1粗1精磁选获得了铁品位为65.78%、回收
率为66.22%的铁精矿,试验结果可以为该铁矿石选别流程确定提供依据。

关键词:

Abstract:

In order to efficiently develop and utilize an iron ore resource in Inner Mongolia,on the ba⁃
sis of the study of the mineralogical properties of ore technology,the whole process of high-pressure roller
grinding,wet magnetic separation,tail throwing,tower mill and magnetic separation was carried out. The
results show that the - 1 mm particle size fine ore was obtained by the high-pressure roller grinding ma⁃
chine,and the wet pre-separation concentrate with a total iron grade of 36.63% and a magnetic iron grade of
31.31% was obtained under the condition of 400 mT,and the wet pre-separation concentrate tower was
ground to -0.030 mm accounting for 95%,and the iron concentrate with an iron grade of 65.78% and a re⁃
covery rate of 66.22% was obtained by one roughing and one cleaning magnetic separation,and the test re⁃
sults could provide a feasible process for the iron ore separation.

Key words:

separation