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现代矿业 ›› 2026, Vol. 42 ›› Issue (02): 250-253.

• 实用技术 • 上一篇    

某选厂铜硫混合精矿再磨段陶瓷球替代钢锻可行性试验

王俊浩,王 飞   

  1. 安徽庐江龙桥矿业股份有限公司
  • 出版日期:2026-02-25 发布日期:2026-03-19

Feasibility Study on Replacing Steel Forgings with Ceramic Balls in the Regrinding Stage of Copper-Sulfur Mixed Concentrate in a Concentrator

  1. Anhui Lujiang Longqiao Mining Co.,Ltd.
  • Online:2026-02-25 Published:2026-03-19

摘要: 针对某选厂铜硫混合精矿再磨段使用钢锻存在的磨矿能耗高、介质单耗大、过磨严重 等问题,开展了陶瓷球替代钢锻的可行性试验研究。通过系统分析铜硫混合精矿旋流器分级沉砂 的化学组成、解离特性及粒度分布,对比了陶瓷球与钢锻在不同充填率、配比及磨矿时间下的磨矿 效果,并进行了浮选对比试验。结果表明:在陶瓷球配比为 m(ϕ30 mm)∶m(ϕ20 mm)∶m(ϕ15 mm)= 30%∶40%∶30%,混合球径 ϕ22 mm,充填率 40% 条件下,陶瓷球磨矿能力优于钢锻,达到相同磨矿 细度(-75 μm 占 72%)时,磨矿时间缩短 15.38%,介质总质量降低 39.49%,能耗仅为钢锻的 51.20%, 且过磨程度减轻 0.89%。浮选试验中,陶瓷球磨矿产品铜精矿铜回收率较钢锻磨矿提高 21.48 个百 分点,硫精矿硫品位和回收率分别提升 2.28 和 11.82 个百分点,中矿量显著减少,有利于工业生产 提高分选效率和流程稳定性。研究表明,陶瓷球替代钢锻在技术经济上具有显著优势,研究结果 可为工业应用提供参考。

关键词: 陶瓷球, 钢锻, 磨矿, 降本增效, 浮选

Abstract: In response to issues such as high grinding energy consumption,high media consump⁃ tion,and severe overgrinding caused by the use of steel forgings in the regrinding stage of a copper-sulfur mixed concentrate at a concentrator,a feasibility study was conducted on replacing steel forgings with ce⁃ ramic balls. By systematically analyzing the chemical composition,liberation characteristics,and particle size distribution of the cyclone underflow from the copper-sulfur mixed concentrate,the grinding perfor⁃ mance of ceramic balls and steel forgings under different filling rates,ratios,and grinding times was com⁃ pared,along with flotation contrast tests. The results showed that under the conditions of ceramic balls ra⁃ tio of m(ϕ30 mm)∶m(ϕ20 mm)∶m(ϕ15 mm) = 30%∶40%∶30%,average ball diameter of ϕ22 mm,and filling rate of 40%,the grinding efficiency of ceramic balls was superior to that of steel forgings. When the same grinding fineness (- 75 μm accounting for 72%) was achieved,the grinding time was reduced by 15.38%,the total media weight decreased by 39.49%,and energy consumption was only 51.20% of that of steel forgings,with overgrinding reduced by 0.89%. In flotation tests,the copper recovery in the copper concentrate from the ceramic ball grinding product increased by 21.48 percentage points compared to steel forging grinding,while the sulfur grade and recovery in the sulfur concentrate improved by 2.28 and 11.82 percentage points,respectively. Additionally,the amount of middlings decreased significantly,which is beneficial for improving separation efficiency and process stability in industrial production. The study dem⁃ onstrates that replacing steel forgings with ceramic balls offers significant technical and economic advantag⁃es,and the findings can provide a reference for industrial applications.

Key words: ceramic balls, steel forgings, grinding, cost reduction and efficiency improvement, flotation